化工进展 ›› 2021, Vol. 40 ›› Issue (S2): 149-155.DOI: 10.16085/j.issn.1000-6613.2021-0638

• 能源加工与技术 • 上一篇    下一篇

火电机组余热梯级供热技术的综合分析

王建勋()   

  1. 国能龙源蓝天节能技术有限公司,北京 100039
  • 收稿日期:2021-03-29 修回日期:2021-04-21 出版日期:2021-11-12 发布日期:2021-11-12
  • 作者简介:王建勋(1983—),男,硕士,高级工程师,研究方向为火电机组故障诊断、性能试验分析、优化运行和节能减排技术等。E-mail:wangjx307@163.com

Comprehensive analysis of cascade heating technology based on waste heat of thermal power units

WANG Jianxun()   

  1. CHN Energy Long Yuan Blue Sky Energy Conservation Technology Co. , Ltd. ,Beijing 100039, China
  • Received:2021-03-29 Revised:2021-04-21 Online:2021-11-12 Published:2021-11-12

摘要:

针对传统供热技术平均?效率低的问题,提出了乏汽余热梯级供热技术。该技术有效地利用了机组乏汽余热,并减少了汽轮机的冷源损失,避免了中排抽汽参数过高造成的能量损失,提高了机组供热经济性。以某电厂为例,本文基于热力学定律与单耗分析理论,建立了乏汽余热梯级供热系统的单耗分析模型,应用该模型对其进行了?分析和附加燃料单耗分析,为节能降耗提供了理论依据。分析结果表明,发电煤耗率由改造前的249.69g/(kW·h)降低到149.9g/(kW·h),降低了99.79g/(kW·h),机组供热负荷较由改造前的788.4MW增加到1673.9MW,增加了885.5MW;改造后传热温差在非严寒期只有7℃、严寒期为26.94℃,比改造前大幅降低;在非严寒期和严寒期,加热器蒸汽入口平均比?比改造前分别降低了524.73kJ/kg、418.2kJ/kg,供热系统的平均?效率比改造前分别提高了51.35%、32.58%,供热系统的平均附加燃料单耗分别为3.11g/(kW·h)、7.98g/(kW·h)。可见通过“乏汽余热梯级供热技术”改造后,节能效果显著,该技术具有广阔的推广应用前景。

关键词: 乏汽余热, 梯级供热, 经济性, 发电煤耗率, ?分析, 单耗分析, 平均?效率

Abstract:

To solve the problem of low average exergy efficiency of traditional heating technology,a cascade heating technology based on waste heat of exhausted steam was proposed.The technology effectively uses waste heat of exhausted steam and reduce the cold source loss of steam turbine, avoid the energy loss caused by the high extraction parameters of steam from intermediate pressure cylinder outlet, and the heating economy of the unit was improved.Taking a power plant as an example,the fuel specific consumption analysis model of cascade heating system based on waste heat of exhausted steam was established based on the law of thermodynamics and fuel specific consumption analysis theory,the exergy analysis and additional fuel specific consumption analysis were carried out by using the model,which provides a theoretical basis for energy saving and consumption reduction.The results indicate that: the coal consumption for power generation decreased from 249.69g/(kW·h) before the transformation to 149.9g/(kW·h),a decrease of 99.79g/(kW·h), the heating load of unit increased from 788.4MW before the transformation to 1673.9MW, an increase of 885.5MW; the heat transfer temperature difference after the transformation was only 7℃ at the non-frigid period and 26.94℃ at the severe cold period, which was much lower than that before the transformation; the average exergy of steam inlet of heater decreased by 524.73kJ/kg and 418.2kJ/kg respectively compare with before the transformation, the average exergy efficiency of heating system increased by 51.35% and 32.58% respectively compare with before the transformation,the average additional fuel specific consumption of heating system was 3.11g/(kW·h) and 7.98g/(kW·h) at the non-frigid and severe cold period.This shows that after the transformation of “a cascade heating technology based on waste heat of exhausted steam”, the economic benefit is remarkable,so it has a broad application prospect in the field of the cascade heating technology based on waste heat of exhausted steam.

Key words: waste heat of exhausted steam, cascade heating, economy, coal consumption, exergy analysis, fuel specific consumption analysis, average exergy efficiency

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