Chemical Industry and Engineering Progree ›› 2016, Vol. 35 ›› Issue (S1): 327-331.DOI: 10.16085/j.issn.1000-6613.2016.s1.053

• Resource and environmental engineering • Previous Articles     Next Articles

Research and application of liquefied petroleum gas (LPG) hydrogen sulfide scavenger

ZHANG Yibin1, FENG Yu2   

  1. 1. Wenchang Oilfield Operation District Co., Ltd. ‘Zhanjiang branch’, CNOOC, Zhanjiang 524057, Guangdong, China;
    2. E-Tech Energy Technology Development Co., Ltd., Tianjin 300384, China
  • Received:2016-02-19 Revised:2016-03-04 Online:2016-07-08 Published:2016-06-30

液化石油气脱硫剂室内研究及应用

张艺膑1, 冯宇2   

  1. 1. 中海石油(中国)有限公司湛江分公司文昌作业公司, 广东 湛江 524057;
    2. 天津亿利科能源科技发展股份有限公司, 天津 300384
  • 通讯作者: 张艺膑(1979-),男,工程师,现从事油气田现场管理工作。E-mail zhangyb5@cnooc.com.cn。

Abstract: Wen13-1/2 oil field liquefied petroleum gas (LPG) recovery project was CNOOC Zhanjiang branch so far the only LPG recycling project, the project had been put into operation so far, had created a good economic and social benefits.In recent years, it sometimes occured that WenChang oil field LPG products copper corrosion test was not qualified.After a series of research and demonstration, copper corrosion exceeding was demonstrated to be in relation of the hydrogen sulfide.Liquefied petroleum gas desulfurization agent Could be a good solution to the problem.This paper discussed the synthetic liquefied gas desulfurization agent, the optimum reaction conditions of:reaction time is 8h, 50% mass fraction of PMA, reaction temperature of 70 DEG C, DEA/MEA mixture of 40% mass fraction, liquefied gas desulfurizer desulfurization rate reached 99.13%.Liquefied gas desulfurization agent in the pH below 5, the reaction temperature was higher than 100 when the desulfurization efficiency will be affected.At a dosage of 50mL/min of Liquefied gas desulfurization agent for 6 months, copper corrosion test decreased from 2a to 1a.LPG products met the national standard requirements.

Key words: liguefied petroleum gas, corrosion, hydrogen sulfide scavenger

摘要: 文昌油田液化石油气(LPG)回收项目是中海油湛江分公司到目前为止唯一一个海上LPG回收项目,项目投产至今,创造了良好的经济效益和社会效益。近年来检测文昌油田LPG产品时而会发生铜腐测试不合格情况。经过现场调研论证发现该铜腐超标和LPG中夹带硫化氢相关。利用液化石油气脱硫剂能够很好地解决该问题。本文讨论了合成液化气脱硫剂的最佳反应条件:合成反应时间8h、PMA质量分数50%、反应温度70℃,DEA/MEA混合液质量分数40%,液化气脱硫剂的脱硫率最高可以达到99.13%。通过以上合成条件,合成了脱硫剂ETTS-1D2。ETTS-1D2在pH低于5,反应温度高于100℃时脱硫效率会受到一定影响。液化气脱硫剂以加注量50mL/min,在现场应用的6个月的时间里,可以有效地将铜腐指标从2a降低到1a。确保LPG产品符合国标标准要求。

关键词: 液化石油气, 腐蚀, 脱硫剂

CLC Number: 

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